already had it done once, it was cause by a worn o-ring letting too much play in the shaft popping the seal... but Matt checked and re-did all the seals he could (whithout taking te box off) and it is still doing it.
it is also only 5th gear and none of the others which makes it less likely to just be low on oil - and the frequency of it popping out is getting higher - 7 times in the last 200miles and at one point it needed 4 goes to pick up 5th again!
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Mods Fitted
Pipercross Filter; Full 2.5" 'Wingy' exhaust; Donny Custom Turbo outlet pipe; Custom injectors;
Uprated gearbox bearings; Helix Clutch; Quaife ATB; Upgraded clutch Hydraulics; FMIC; Ported Head; ARP headstuds; Leda coilovers; 'Brembodge' 326mm disks/DS2500 pads
Dieselpowered
Fitting Custom Hybrid Turbo (1856GTBv) & controller; Remap, swirlpot, lift pump
AMW Motorsports
Custom exhaust manifold & downpipe
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